NTSB Identification: ERA16FA194
14 CFR Part 91: General Aviation
Accident occurred Tuesday, May 24, 2016 in Rhoadesville, VA
Aircraft: JIHLAVAN AIRPLANES SRO KP 5 ASA, registration: N440JM
Injuries: 2 Fatal.
This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators either traveled in support of this investigation or conducted a significant amount of investigative work without any travel, and used data obtained from various sources to prepare this aircraft accident report.
On May 24, 2016, about 1625 eastern daylight time, an experimental light sport Jihlavan KP 5 ASA (Skyleader 500), N440JM, was destroyed when it impacted terrain in Rhoadesville, Virginia. The sport pilot/owner and the flight instructor were fatally injured. Visual meteorological conditions prevailed, and no flight plan had been filed for the local flight from Culpeper Regional Airport (CJR), Culpeper, Virginia. The instructional flight was conducted under the provisions of 14 Code of Federal Regulations Part 91.
According to a friend of the sport pilot/owner, he had recently purchased the airplane, and had it ferried from California to CJR. The sport pilot was required by his insurance company to have 4 hours of dual operation before being able to fly the airplane solo. CJR records indicated that the airplane arrived on May 13, 2016, and the sport pilot's logbook indicated that he had flown the airplane twice on May 20, 2016, for a total of 2.5 hours, with "dual received" flight time noted for both flights.
According to Federal Aviation Administration (FAA) sources, no air traffic control services were provided. However, radar returns indicated that after departing CJR about 1530, the airplane headed southwest to Orange County Airport (OMH), Orange, Virginia. There, radar indications disappeared and reappeared four times, consistent with approaches below radar coverage to runway 26. After the fourth approach, the airplane proceeded northeast, and later turned east before disappearing from radar. There were no altitude readouts from the airplane during the entire flight.
According to several witnesses near the accident site, they heard what sounded like thunder or a "crack." They then saw a parachute deployment and the airplane nosed straight down before impacting the ground. Witnesses could not determine the airplane's altitude at the time other than it was low, or whether the engine was operating.
The wreckage was located on open terrain in the vicinity of 38 degrees 15.917 minutes north latitude, 077 degrees, 51.465 minutes west longitude, at an elevation of about 400 feet. The airplane was found upside down and complete, with the exception of some smaller pieces in close proximity. When the airplane was righted, significant fore-to-aft crushing damage was noted to the nose section and to both wings.
The airplane was subsequently moved to a temporary storage facility where it was laid out and the presence of all flight control surfaces was confirmed, as was control continuity from the each flight control surface to the cockpit controls.
The airplane was equipped with a ballistic parachute system. The ballistic parachute system included a fabric canopy attached to the airframe via four metal-wire risers. Two of the risers were individually attached to the airframe via their respective anchors, while the other two risers were together attached to a third airframe anchor. A drogue parachute assisted in main parachute deployment.
At the accident scene, the drogue parachute was found in a nearby field and the main parachute was found in trees about 100 yards east of the wreckage. At the temporary storage facility, the parachute's fabric canopy was spread out and observed to be undamaged. The two individual risers were found to be separated near their respective airframe anchors with the wire ends broomstrawed, consistent with overload separation. The other two risers were found still attached to their single anchor; however, that anchor was itself separated from the airframe. The cockpit parachute activation handle appeared pulled (system was activated.)
The airplane was subsequently moved to a long-term aircraft storage facility.
Due to the extent of observed damage and heavy mud impaction, the engine was not examined at the temporary facility but will be at the long-term facility.
There were no dedicated recording devices onboard the airplane; however, there were some avionics that could have retained non-volatile data. The heavily damaged avionics were removed, and data downloads will be attempted.